|
Home | Rules & Guidelines | Register | Member Rides | FAQ | Members List | Social Groups | Calendar | Mark Forums Read |
Builds (and builds only) Got a build thread? It goes here, build threads anywhere else on the forum will be locked and never moved. |
|
Thread Tools | Display Modes |
02-05-2013, 12:28 AM | #1 |
$900 Junky to Megasquirted ka swap
IMG_0661.JPG
17 years old and quickly growing into the drift scene, I decided I wanted something fun to drive and easy to work on for a first car. After a full summer of working my but off at minimum wage and searching for cheap deals on craigslist, I came across a 90' s13 hatch going for $1,200. Lucky for me when I got there, a few problems were brought to my attention that I hadn't known about before. I leaky radiator, screaming fartcan of an exhaust, oil leak, crunchy transmission, all the goodies. But it drove alright and I was eager to get it. I talked this guy down to 900 bucks and drove it home the same day. IMG_0890.JPG IMG_0525.JPG So I drove the crap out of it for two weeks and it crapped out on me thanks to the cooling system. Blown head gasket, coolant spraying out of spark plug holes, not a good thing. So here I was, not knowing much about engines, pretty much stumped. Luckily for me, I have an uncle that is the CEO of a standalone manufacturing company, MegaSquirt | Engine Management System | Electronic Fuel Injection - DIYAutoTune.com, who was glad to help get this thing running again. So we towed the car up to his shop, and I decided to take advantage of this and swap in a dual cam ka. My uncle found a steal from one of the shops down the street for a lightly used one talking them down to $100. We pulled the single cam out of the bay and I got to the prep work. IMG_0638.JPG IMG_0639.JPG Then started gutting the engine bay. IMG_0654.JPG There was a rusted out spot in the bay from the battery so we cut it out and did some work to it. IMG_0647.JPG IMG_0733.JPG After that we stripped down the other engine and sent the block and head to be resurfaced and honed. IMG_0687.JPG We went with single cam piston heads, giving the compression of 12:1 IMG_0775.JPG We got the block and head back and I readied it for paint. IMG_0879.JPG Then painted and the assembly began. IMG_0871.JPG Went with two exhaust cams, supposed to give more upper end torque. Getting shim measurements were a pain in the nads. IMG_0877.JPG Clean looking engine. IMG_0977.JPG IMG_1018.JPG Besides me bench pressing the tranny while lowering it in, it went pretty smooth. I took some Altima fans, disassembled them, trimmed, painted, then mounted on a Koyo Radiator. IMG_1051.JPG http://zilvia.net/f/attachments/buil...p-img_1001.jpg Last edited by caseyculby; 02-07-2013 at 12:45 AM.. |
|
Sponsored Links |
02-06-2013, 10:21 PM | #2 |
Thank god for Ms3.
So now, it's been a month since I got it from the shop. My uncle had done a custom engine harness and tuck, all running through the new Ms3 Megasquirt system. We ran it on the dyno a bit and had it tuned within an hour. I got it home and had to get emissions passed on it, first try failed, went home, tuned it from my laptop in my driveway. Next day I came in, I passed.
|
|
Bookmarks |
Tags |
ka24de, rebuild, s13, s14, swap |
Thread Tools | |
Display Modes | |
|
|