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S Chassis Technical discussion related to the S Chassis such as the S12, S13, S14, and S15. |
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01-19-2013, 06:09 PM | #1 |
Join Date: Aug 2012
Location: Tampa FL
Age: 30
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Help Please: SR20DET Fuel Cut / Popping
So, my issue is as listed above, I'll begin with a mod list. All of which are around 3 and a half months old.
FMIC (no-name) CircuitSports hotpipe HKS SSQV3 Megan 3" DP 3" no name exhaust TurboSmart boost gauge Walbro 255lph pump Running z32 fuel filter and NGK plugs with a 6 heat rating (copper) gapped to .032 Tested piping to 20psi and fixed one very minor boost leak. I'm only running stock 7psi but for some reason I can run it to 5-6 psi at probably 60% throttle with no problems but as soon as I go near WOT, it goes very hesitant with a rapid backfiring and jumping boost reading between 3 and 15ish pounds. replaced coolant temp sensor and plugs are new. another slight problem I'm having is as soon as I hit operating temperature (3rd notch on gauge) it stumbles a couple times and then picks back up which leads me to believe o2 sensor is a possibility. Vacuum is at a steady 20inhg at idle btw. Going to give the o2 a try but if thats not it, im at a loss. Please give any insight if any of you have had this happen to you. Any help is appreciated. Thanks. Also.. I've tested my TPS and its throwing correct voltage closed and open. Last edited by chase_gavin; 01-20-2013 at 11:09 AM.. Reason: Update |
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01-21-2013, 02:34 PM | #5 |
Zilvia FREAK!
Join Date: Nov 2010
Location: arizona
Age: 33
Posts: 1,519
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Gap plugs down to .028. I would get blow out with the weak srcoils if I was gapped any larger.
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01-21-2013, 02:47 PM | #6 |
Zilvia Member
Join Date: Jun 2012
Location: porterville
Age: 28
Posts: 157
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I was also running a hks bov and I had the same problem what was happeing was once it hit full boost at wot the bov would start leaking...........what I did I grabbed a a straight inteercooler pipe. That I had laying around in my back yard and replaced it with the pipe. That was holding my snapring type bov and blocked off the vaccum line that runs to the bov with a screw To make sure it was the bov and car ran fine.......pretty much eliminat the bov or replace it with another one that you know works
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01-21-2013, 06:11 PM | #7 |
Join Date: Aug 2012
Location: Tampa FL
Age: 30
Posts: 28
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Feedback Score: 0 reviews
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Not too familiar with the term "blow out" but i am going to give them a shot gapped down a bit. I've heard from a few people now that ideal gap is .028. Also going to give a new knock sensor a shot since I managed to get an OEM Nissan unit for $18.
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01-21-2013, 06:15 PM | #8 |
Join Date: Aug 2012
Location: Tampa FL
Age: 30
Posts: 28
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Thanks for all the help guys. I appreciate it. Fairly new to the Nissan world but I'm liking it so far. Bought my s13 coupe 6 months ago, did my first SR swap 4 months ago, VLSD swap a month ago, now just getting it back running right and going for a 5lug swap with Q45 front brakes and 17x8.5 Gram Light 57C's. Project is coming along well all thanks to good friends and some elbow grease.
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01-21-2013, 06:20 PM | #9 | |
Join Date: Aug 2012
Location: Tampa FL
Age: 30
Posts: 28
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Feedback Score: 0 reviews
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Quote:
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01-21-2013, 07:05 PM | #10 |
Zilvia Member
Join Date: Aug 2011
Location: westchester NY
Age: 32
Posts: 232
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Feedback Score: 4 reviews
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stock boost is 11psi not 7
get the stock boost solenoid to run stock pressure
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01-23-2013, 06:46 PM | #13 | |
Leaky Injector
Join Date: Dec 2012
Location: van alstyne, tx
Age: 27
Posts: 110
Trader Rating: (1)
Feedback Score: 1 reviews
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Quote:
and glad to see you got it fixed |
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Tags |
backfire, boost cut, fuel cut, popping, wot |
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