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Engine Tech Technical discussion related to all relevant engines such as KA, SR, RB, CA, 2JZ , L24/26/28, VG, VQ, and LSx series. |
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09-22-2009, 03:21 PM | #33 | |
Zilvia Addict
Join Date: Mar 2006
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i did that already... fail at reading...lol thanks guys, any more?
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09-22-2009, 06:54 PM | #34 |
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Did you try replacing the maf like I described earlier with one that is known to work perfectly. Most times when a maf is bad maf cleaner doesnt do shit.
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09-22-2009, 06:59 PM | #35 | |
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Swap upper harnesses with someone.
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09-22-2009, 09:30 PM | #37 |
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apparently he is not desperate enough yet. haha
the funny thing is 7 out of ten times I fix this type of issue within like 10 minutes of showing up its alwasy something super simple/stupdi
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09-22-2009, 10:16 PM | #38 | |
Zilvia FREAK!
Join Date: Dec 2007
Location: 626DRIFT, ca
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But I am wishing its a broken or collapsed valve spring(s). If it is floating valves, I can build chucks engine and get him the extra power hes always wanted. Not quite M. Essa power but enough for now. Might as well build the rest of Team Mulsannes engines since everyone is having problems. Barrow my hoist and bring me your engine... and Codys and Teddys. 1 1/2 weeks left chuck. ~m
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09-22-2009, 11:32 PM | #39 |
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lol nice.
As long as you send him to me for mechanical / boots controller tune up on my dyno you can handle the rest of his mess.
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09-23-2009, 12:06 AM | #40 | |||
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i swapped coilpack harnesses with my roommate, but nothing. me and gary pulled the entire motor harness earlier today before work to go through it just in case, to rule that out. tmw's another day, we'll see how it goes.
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thank goodness cody has a spare motor i'm bumming parts off. thanks cody! Quote:
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09-23-2009, 12:52 AM | #41 | ||
Zilvia FREAK!
Join Date: Dec 2007
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~m
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09-23-2009, 11:25 PM | #43 |
not giving a fuck
Join Date: Apr 2007
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have you check the TPS ... MehSilvia is having horrible bog issues, similar to urs...he already figured out it was TPS he checked voltage and it was horribly wrong...change he TPS...
im pretty sure that can be it... since it affects air/fuel mixture... him being N/A and u boosted could result in diff results
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09-24-2009, 12:50 AM | #45 |
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Still sounds like the right person hasnt really diagnosed it honestly man, no offense.
It can only be so many things. The car is a mechanical object. 1+1 = 2 everytime. If you can get the car down to LB ill only charge 40 bones and ill give it a check and give you my honest opinion. eitherway I would check compression AGAIN and AGAIN and AGAIN Also if you wiring harness has ANYTHING WRONG AT ALL that you can see, like shotty wiring or grounding shroud or crap or any butt connectors I would throw it i the trash and get a new harness in better shape or better yet just get a brand new wiring harness and start over. This was the best thing I ever did on my last S13, I just ponied up and almost all of the intermittent electrical bugs were totally gone forever, car ran a lot better
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09-24-2009, 03:27 AM | #47 | |
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Problem is, he won't be able to easily get the car down to Long Beach. High 12's I think he said, unless I'm thinking about someone else I was helping. Coulda been Nick I was talking about batt voltages with.
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09-24-2009, 05:13 AM | #48 |
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Maff
turbo blown leak ive had the symptoms that you had with all three. or coilpacks, but youve checked that.
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09-24-2009, 11:09 AM | #50 | |||
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hows the idle?
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