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Breitling
04-17-2012, 07:59 PM
Well,

I just installed a new Grimmspeed Manual boost controller on my s14 240sx (Redtop SR20)

Backstory; Prior to tonight i had removed the old hallman MBC in efforts to trace down a Fuel pressure issue. Fixed the fuel pressure issue while the internal T28 wastegate was linked directly to the 50mm tial BOV and it was getting a dead-nuts factory 8 PSI (factory waste gate setting)

Tonight I put the new MBC inline and loosen it so that the boost controller is all the way "undone" and now the car is boosting to like 20 LBS of boost when i test drove it. my thought is that with the boost controller all the way loosened i should be right at 8psi... no?


Things i noticed.....

the vac line going from the wastegate to the MBC is "split" into one of the vac fittings on the intake throttle body..... could this be the problem? if so. how come it didn't affect it with just the wastegate & 8psi scenario.

HELP

Breitling
04-17-2012, 08:32 PM
BTW... heres how its hooked up...is the MBC backwards?

http://sphotos.xx.fbcdn.net/hphotos-snc7/319832_10100764744048824_23307162_51722905_1463275 788_n.jpg

ultimateirving
04-17-2012, 08:54 PM
looks backwards to mee, you want the side with the little ball bearing, connected toward the T/b, so the boost can blow past it once it reaches desired psi. If its backwards it will never open causing super boost.

cotbu
04-18-2012, 06:36 AM
looks backwards to mee, you want the side with the little ball bearing, connected toward the T/b, so the boost can blow past it once it reaches desired psi. If its backwards it will never open causing super boost.

Good catch. If it's hooked up like that, I guarantee that's the problem!